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Body work – time to repair some SMC

Body work – time to repair some SMC

The classic GMC motorhome body is made up of aluminum and fiberglass-like material called SMC (Sheet Moulded Compound). The front and rear “caps” of the motorhome and the sides below the “waist” and made of SMC. SMC, like fiberglass, is somewhat brittle and when tires come apart, like they occasionally do on motorhomes, the SMC cracks and breaks when it is hit by the disintegrating tire. “Barbie” had some damage from a tire failure when we bought it – Uncle Dave had the right-rear tire come apart and make a hole in the propane door and the fender just in front of it. Since then we have had two more instances of tire failures – one on the same wheel as Uncle Dave’s and another on the middle wheel on the driver’s side. The driver’s side one did more damage there.

This post is going to cover the repair of the propane door. I intend to take some more photos of the fender just in front of the propane door when I begin that repair next week. I worked a little with fiberglass when I was a starving student in Omaha and had to repair a badly rusted VW bus but I really didn’t know much about it. I read all I could from the various GMCnet sources, I watched a few youtube videos and went to Finishmaster, our local auto-body supplier for some advice. They sell the Evercoat line of products for SMC and, after 3 trips, one for each phase of the repair, I have a nicely repaired propane door. Total material costs so far are about $210 for the supplies which should be enough to fix all the holes in the SMC – I hope.

 

 2013-09-14 12.31.30  This is the way the propane door and the fender just in front of it looked when we bought the coach. The tire had come apart on Uncle Dave and done this damage.
2013-09-14 12.31.07  Closeup of the damage.
 2014-01-29 09.46.22  Once I had the door off I found that there was more damage than previously visible. The rear corner and latch was almost completely broken off. Things I saw on youtube suggested using a grinder and opening up serious cracks and breaks so I did. I used some scraps of Formica-type material as backing, bent them using a heat gun and then glued them into place using the epoxy resin for the SMC.
 2014-01-29 09.47.14  This is a view of the back side of the repairs showing the plastic backing that was epoxied into place and shaped using heat. The curve was made to match the fender-repair piece (next phase of the repair) that Fay Curtis supplies.
 2014-01-29 09.47.39  A closer-up photo of the back of the repair.
 2014-01-29 09.47.48  Support for the “crack” at the rear of the door. It also was epoxied into place.
 2014-01-29 14.46.35  This is after the first “layup” of epoxy resin and glass fabric was put over the “crack” at the rear of the door and supported by the Formica backing. I think that this was 2 or 3 layers of thick glass matting and resin.
 2014-01-29 14.46.42  This is after the first “layup” of epoxy resin and glass fabric was put over the big hole and sanded off. This was after 2 – 4 layers of thick glass matting and resin.
 IMG_0005  This is the second layup on the crack at the rear of the door. The objective here is to bring the area up to near the finished level
 IMG_0006  This is the second layup on the missing section. Also trying to bring this up to the finished level – another 2 to 3 layers, more in one spot.
 IMG_0008  This is the SMC resin that I have seen recommended on the internet and by my local supplier. The little white tube is the hardener – a very small percentage is used in the mix.
 IMG_0035  There were a couple of small cracks developing around the vent louvers so I decided by reinforce the frame around them in the back. In the front, I opened up two cracks with a sander so I could use some filler on them.
 IMG_0038  This is the next coat as recommended by the Evercoat company and by my local supplier. It can be used as an adhesive or filler. It sets up fast even in (Arizona) cool weather but does a great job of filling. It took two or three thin layers to get the low spots filled.
 IMG_0039  This is the door after the filler was applied the last time.
 IMG_0040  This is the door after sanding the filler for the final time.
 IMG_20140131_105444_310  I used a Forstner bit to re-open the holes for the latches. I ordered a set of stainless steel latches from Applied GMC.
 IMG_0047  I bought a can of beige SEM primer and gave the “finished” door a light coat and was shocked to see lots of little pin holes and minor defects show up that I could not see before. Another visit to the supplier resulted in the purchase of this glaze that fills those minor defects. I was told that this was the normal process – it takes a coat of primer to see what you have missed.
 IMG_0047 cropped  Here is a closeup so you can read the label.
 IMG_0048  Here is the final product, ready for reinstallation.
 IMG_0049  This is the fender repair piece that Fay Curtis makes. I used it as a guide to match the curve for the missing piece. The next phase of the project is to install that fender repair piece.

The 2014 Agri-Country Bluegrass Festival

The 2014 Agri-Country Bluegrass Festival

IMG_4466
This is our 40th trip in our GMC. Yes, it is kind of short but we are staying in it 3 nights so it is a trip. We are basically dry camping because the electricity keeps going out. Something is wrong in the main box or lots of RVs are drawing too much power. Since it has not happened here before for us I am leaning toward the main box.

This festival gets better each year. They bring in about 4 well-known bands and each of them does about 4 performances over a 2-day period. There are performances beginning at 9 or 10 a.m. Friday, Saturday and Sunday. There are lots of other bands that perform every day and all are great. There is also a car show on Saturday and a tractor pull which we have never seen – just too busy listening to the music.

Here are some photos – forgive the blurry ones. I need a new camera.

 

A good trip home but something is amiss

A good trip home but something is amiss

After watching lots of balloons take off (ascend) on Sunday morning we decided we saw enough and it was time to head for home. The coach ran great the whole way but for the last hour or hour and a half of the 6-hour trip we had a sort of whistling noise coming from somewhere up front. At first I thought it might be either the power steering pump or the alternator but a little experimenting convinced me that it is probably a vacuum leak somewhere. The noise completely disappeared below 60 mph and, above 60 mph I could make it come and go with the gas pedal. The vacuum gauge did not seem to be any different than normal so I didn’t worry about it.

Once we got home and unpacked – not completely since we will be leaving again in 4 days – I moved the coach to the parking lot (can’t park on the street overnight) and it ran like there was some sort of fuel problem – I had to keep working the gas pedal to keep it running. At first I didn’t connect the whistling noise to this problem but now I am thinking that the hour or so parked in front of the house allowed the engine to cool enough that the theoretical vacuum leak affected the advance or choke mechanisms. I will inspect all of the hoses later this morning to see what I can see.

Well, nothing wrong that I can tell right now. I inspected all of the hoses and nothing is off where it should be and all of the hoses are fresh and solid. The coach started right up and ran great getting back over to the house. The next trip is only about 50 miles each way so not much risk there. More later if there is anything to report.

Update 1/27/2014: The rough running went away for some reason. When I went back to get the coach the next morning I checked all of the vacuum hoses and connections and could find no problem. The hoses are very new and all connected solidly. The whistling noise I now believe to be coming from the power steering pump and maybe it is more of a high-pitched whine than a whistle. Time for a new one I think.

Ho Hum – more balloons

Ho Hum – more balloons

 When we got up this morning  we had to start the generator to recharge our batteries. Our clock which projects on the ceiling, was so low on power during the night that you couldn’t even read it. We both thought there was something wrong with our eyes. There were other generators running and we felt bad about the noise but we had to do it.

It turned out to be a really beautiful day and there were a bunch of balloons up by 8 am as opposed to yesterday when it took them a while to get stirring. We took a walk down by the marina again trying to get a view of balloons touching the water but no luck. I think the place to go to see them in the water is over where the water goes under the London Bridge.

We made the mistake of leaving the campground in the Tracker for a “quick” trip to the store around noon. That was a mistake. There was a line a mile long of bumper-to-bumper cars heading right past our campground toward the main entrance to the event. It took us about 45 minutes to get back “home” after our “quick” trip.

We made another trip back to the event but this time we walked – on prior trips we drove the Tracker to the free parking lot and then walked the last quarter-mile. It was a pretty comfortable walk along the shoulder of the road and probably made up for that huge sandwich I had for lunch while there.

We spent the afternoon napping and reading. We may or may not go back over there tonight but probably not. Heading for home tomorrow morning.

Arrival and first day at the balloon festival

Arrival and first day at the balloon festival

We left home at about 9:00 am got to Lake Havasu City at about 3:00 pm without any trouble at all. The weather was nice – it never got above 78 and it wasn’t very windy at all. We took our usual route around Phoenix via highway 85 between I-8 and I-10. We get off the interstate about 40 miles short of Quartzsite and go directly toward Parker and up highway 95 to Lake Havasu City. We missed the detail that the turn onto London Bridge required being on a parallel street and that was our only “problem” all day. We cruised at about 63 mph (it felt good) all day and the coach ran like a top.

We arrived at the parking lot where we will spend the next 3 nights and it was wide open – not crowded at all. The problem was we didn’t know where the activities would be so where we should park. We finally settled on a row of spots that are back-in only and less desirable to minimize the number of neighbors – some people are jammed in next to each other.

We spent a nice quiet night – quiet time is after 10 pm and there were lots of generators before then, this is dry camping only for $20 per night. The schedule said that the “mass ascension” would be at 7:45 am so we got up and dressed so we could sit at the far corner of the parking lot. By 8 am there was only one balloon showing at the “balloon field” so we shrugged our shoulders and headed back to the coach for some breakfast and coffee. Walking back we saw a good half-dozen balloons being inflated in the area immediately in back of our coach. It turns out that the balloons launch from all over town – any empty parking lot they can find. There is no better spot to watch than the one we chose.

We watched from 50 to 60 balloons fly out over the lake and back again on a wonderful morning, warm and calm. We wandered around the festival area which is on a golf course and arranged in a large circle around the “balloon field” which is actually pretty small as balloon fields go I think.

Tonight, just after dark, they are supposed to do a “night glow” but it is iffy because of wind. Right now (2 pm) it is a little windy and yesterday it was very windy. We are hoping – had the same problem in Albuquerque in 2009 and no evening or morning events happened.

List of all (or most anyway) repairs and upgrades to our ’76 Eleganza II

List of all (or most anyway) repairs and upgrades to our ’76 Eleganza II
Date Vendor Description Cost Mileage Owner
01/24/94 Southland Enterprises Buford, GA radiator, transmission & oil cooler lines, transducer, alternator 46661 Jim Bowles
02/25/94 Southland Enterprises Buford, GA fan clutch, transmission governor, exhaust system 46994 Jim Bowles
06/09/94 Southland Enterprises Buford, GA master cylinder, fuel lines 49694 Jim Bowles
08/30/94 Southland Enterprises Buford, GA RH cv joint & boot 51818 Jim Bowles
09/26/94 Southland Enterprises Buford, GA LH wheel bearing, knuckle and lower ball joint 52034 Jim Bowles
05/12/95 Camping World Heat strip for Duotherm Howard Black
01/10/97 fuel hoses
02/04/97 NAPA CV Joint boot 2456SB
03/19/97 Sams Club tires 60203 Jack Benson
04/01/97 NAPA Steering boot kit UVB101 13.00
04/17/97 Clasco Manufacturing Corp Front end – steering column master bearing, drag link, idler arm, tie rod ends and adjusters, relay lever, upper control bushings, lower arm control bushings, upper and lower ball joints 2,500.00 Jack Benson
06/26/97 Camping World Aqua Magic toilet
08/03/97 CarQuest alternator 156.00
03/24/98 Golby Motor Corp Front and rear brake hoses 181.00 Jack Benson
04/01/98 steering column bushings and bearing
04/24/98 Camping World Dometic RM2652 2-door refrigerator 949.00
07/10/00 Golby Motor Corp 9# radiator cap 10.00
08/21/00 Golby Motor Corp Air bags (2) 530.00 75890 Jack Benson
05/17/02 NAPA heater blower motor relay Patrick Loe
05/22/02 Alex Sirum GMC headlight kit 225.00 Patrick Loe
05/31/02 Golby Motor Corp Grille, door latch, holding tank sender 438.00 Patrick Loe
06/17/02 Alex Sirum GMC water tank sender 121.00 Patrick Loe
07/17/02 Ramco Ramco mirrors 411.00 Patrick Loe
09/16/02 Alex Sirum GMC Install complete macerator system 300.00 78906 Patrick Loe
09/16/02 Alex Sirum GMC complete front brake upgrade – new rotors, 80mm calipers, hoses, carbon metallic pads 531.50 78906 Patrick Loe
09/16/02 Alex Sirum GMC replace both windshields 1,050.00 78906 Patrick Loe
09/17/02 Alex Sirum GMC Trailer hitch – thru bumper 250.00 78906 Patrick Loe
09/17/02 Alex Sirum GMC 3.55 final drive 1,250.00 78906 Patrick Loe
09/17/02 Alex Sirum GMC rear brakes, new Delco shoes, new o/s cylinders 206.00 78906 Patrick Loe
09/17/02 Alex Sirum GMC KYB shock absorbers (6) 297.00 78906 Patrick Loe
11/20/06 Uncle Dave original purchase 10,000.00 81041 Armand & Carol Minnie
11/27/06 Simonson Generator tune up Onan generator 322.48 Armand & Carol Minnie
02/13/07 B&B auto repair fix leaking radiator 477.49 Armand & Carol Minnie
03/06/07 Cinnabar Propane tank sender 52.84 Armand & Carol Minnie
03/31/07 Armand replace hoses from engine to water heater Armand & Carol Minnie
05/21/07 Duane Simmons electronic cruise control – installed by AJM 265.00 Armand & Carol Minnie
06/20/07 Arizona Mobile Mechanic replace rear main seal on original engine 932.00 90579 Armand & Carol Minnie
07/10/07 Arizona Mobile Mechanic repair L/H exhaust manifold 180.00 92095 Armand & Carol Minnie
07/16/07 All RV new roof air and misc b.s. 1,133.76 92133 Armand & Carol Minnie
07/18/07 Arizona Mobile Mechanic repair & recharge A/C 275.00 Armand & Carol Minnie
08/21/07 Taylor Chevrolet – Rexburg, ID Replace engine – Motor Works, Spokane, WA 5,938.00 94515 Armand & Carol Minnie
08/21/07 Taylor Chevrolet – Rexburg, ID Check transmission 187.04 94515 Armand & Carol Minnie
09/17/07 Lube-it Express Moab, UT change oil 34.43 95020 Armand & Carol Minnie
09/24/07 Arizona Mobile Mechanic replace choke heater tube 74.85 96415 Armand & Carol Minnie
09/24/07 Arizona Mobile Mechanic replace all rubber fuel lines and filler hose 403.25 96415 Armand & Carol Minnie
09/24/07 Arizona Mobile Mechanic replace air filter 12.25 96415 Armand & Carol Minnie
09/24/07 Arizona Mobile Mechanic check brakes – over 50% worn 25.00 96415 Armand & Carol Minnie
09/24/07 Arizona Mobile Mechanic replace turn signal switch & 4-way 118.89 96415 Armand & Carol Minnie
12/03/07 Costco tires 1,305.84 96450 Armand & Carol Minnie
12/04/07 Arizona Mobile Mechanic fix r/h exhaust manifold noise 156.00 96459 Armand & Carol Minnie
12/10/07 Applied GMC Eagle wheels (7) 1,225.00 96450 Armand & Carol Minnie
12/10/07 Applied GMC T-skirts & brackets 95.00 Armand & Carol Minnie
01/11/08 Arizona Mobile Mechanic fuel tank not switching properly 114.56 98861 Armand & Carol Minnie
01/11/08 Arizona Mobile Mechanic fix r/h exhaust manifold noise 138.33 98861 Armand & Carol Minnie
01/11/08 Arizona Mobile Mechanic fix exhaust leak in choke heater 90.50 98861 Armand & Carol Minnie
11/27/08 Coop motor works Onan board 223.00 Armand & Carol Minnie
12/03/08 Arizona Mobile Mechanic change brake fluid – repack rear wheel bearings 417.95 101557 Armand & Carol Minnie
04/14/09 replace macerator pump (again) macerator pump 125.99 Armand & Carol Minnie
05/07/09 Applied GMC electric fuel pump kit 186.00 Armand & Carol Minnie
05/07/09 Applied GMC digital monitor panel 96.70 Armand & Carol Minnie
05/07/09 Applied GMC APC cable 25.00 Armand & Carol Minnie
05/07/09 Applied GMC city water fitting 35.79 Armand & Carol Minnie
06/02/09 Applied GMC transmission vent – hose 18.50 Armand & Carol Minnie
06/02/09 Applied GMC Lumina Wipers and blades 84.95 Armand & Carol Minnie
06/02/09 Applied GMC Buttons and screws for window 3.00 Armand & Carol Minnie
06/03/09 Arizona Mobile Mechanic install electric fuel pump 465.96 104097 Armand & Carol Minnie
06/03/09 Arizona Mobile Mechanic fix transmission leak – still leaking from front 211.80 104097 Armand & Carol Minnie
07/14/09 AJM install house battery shutoff 30.00 Armand & Carol Minnie
07/14/09 AJM install Intellipower PD9245CV power converter 172.32 Armand & Carol Minnie
07/14/09 AJM install city water fitting – take insides out of original check valve 10.00 Armand & Carol Minnie
07/14/09 AJM change oil – Mobil 1 – NAPA filter 104097 Armand & Carol Minnie
09/16/09 AJM Digital monitor panel – installed Armand & Carol Minnie
11/06/09 Applied GMC replace oil cooler lines with JR Slaten’s SS setup 230.00 107400 Armand & Carol Minnie
11/06/09 Applied GMC replace left outer CV joint & boot 107400 Armand & Carol Minnie
11/06/09 Applied GMC replace right knuckle 107400 Armand & Carol Minnie
11/06/09 Applied GMC replace steering damper 107400 Armand & Carol Minnie
11/06/09 Applied GMC replace end link bushings 107400 Armand & Carol Minnie
11/06/09 Applied GMC replace sway bar bushings 107400 Armand & Carol Minnie
11/06/09 Applied GMC replace both lower ball joints 107400 Armand & Carol Minnie
11/06/09 Applied GMC replace bearing on left intermediate axle 107400 Armand & Carol Minnie
11/06/09 Applied GMC repack rear bearings 107400 Armand & Carol Minnie
11/06/09 Applied GMC replace brake shoes on both intermediate wheels 107400 Armand & Carol Minnie
11/06/09 Applied GMC replace brake cylinder on right intermediate wheel 107400 Armand & Carol Minnie
11/06/09 Applied GMC replace plugs, rotor, distributor cap, ignition wires 107400 Armand & Carol Minnie
11/06/09 Applied GMC replace alternator 107400 Armand & Carol Minnie
11/06/09 Applied GMC replace both front bearings add zerk fittings 107400 Armand & Carol Minnie
11/06/09 Applied GMC replace transmission with Manny rebuild 2,298.00 107400 Armand & Carol Minnie
11/06/09 Applied GMC Change oil and filter (wix filter) 70.00 107400 Armand & Carol Minnie
11/11/09 Applied GMC install dual bag rear suspension system 1,231.00 108000 Armand & Carol Minnie
11/11/09 Applied GMC replace mufflers 108000 Armand & Carol Minnie
11/11/09 Applied GMC replace steering boot 108000 Armand & Carol Minnie
11/11/09 Applied GMC replace fuel pump – pressure too high 0.00 108000 Armand & Carol Minnie
11/11/09 Applied GMC replace carburetor with Patterson rebuild 514.00 108000 Armand & Carol Minnie
11/11/09 Applied GMC replace transmission with Manny rebuild – first one failed 0.00 108000 Armand & Carol Minnie
12/01/09 Replace driver’s side windshild with new gasket 108000 Armand & Carol Minnie
12/30/09 Arizona Mobile Mechanic final drive – new seals and gaskets 434.00 109352 Armand & Carol Minnie
04/05/10 AJM install VIAIR compressor and all metal fittings 85.00 111868 Armand & Carol Minnie
04/06/10 Dave Lenzi ride height adjusters 61.00 111868 Armand & Carol Minnie
04/06/10 AJM rotate tires – spare to RF – clockwize – LF to spare 111868 Armand & Carol Minnie
04/06/10 Springfield Ignition Replace distributor & add timing tab (missing from rebuilt engine) 111868 Armand & Carol Minnie
04/28/10 AJM install Shurflo Whisper King water pump 92.22 111868 Armand & Carol Minnie
07/15/10 Arizona Mobile Mechanic install aluminum radiator 1,200.00 114582
07/31/10 AJM remodel interior living space 5,000.00
01/01/11 AJM upgrade rear suspension to quad-bag 500.00
08/01/11 AJM upgrade rear brakes to discs with reaction arm 5,000.00
02/07/12 AJM fuel/vapor separator & charcoal cannister 200.00
02/08/12 AJM stainless hot water heater 300.00
02/10/12 AJM aqueous foam fire extinguisher in engine compartment 400.00 17,615.22
02/21/12 AJM new switches for lights and water pump including in bath 100.00
03/03/12 AJM r & r intake manifold to install blocking plates on exhaust crossover
03/03/12 AJM belt tensioner on A/C compressor 25.00
03/03/12 AJM install Remflex gasket on passenger side exhaust manifold
03/30/12 AJM two new Magnaflow SS mufflers and 2 1/2″ pipe from mufflers back including new “Y” 495.00
04/02/12 AJM ventilation – with remote control blast gates
belt tensioner on alternator 70.00
04/15/12 AJM aux. vacuum pump for brakes
04/15/12 AJM new belts on alternator and a/c 20.00
04/15/12 AJM new fresh-air ventilation 100.00
06/10/12 rebuilt transmission purchased from Steve Ault 600.00
06/11/12 NextGenAuto install transmission 588.00
07/03/12 NextGenAuto install new seals in final drive and fix engine oil leaks 300.00
07/03/12 NextGenAuto replace A/C compressor, hose, and recharge w/R134 1,049.00
07/05/12 AJM fabricate and install center console in cockpit
AJM install transmission temperature gauge
07/12/12 AJM replace Onan mount cushions to fix sag
09/06/12 AJM replace tires (6) 866.00 142000
11/27/12 AJM replace driver’s side outer CV boot, shockmount grommet, install transmission cooler, replace spark plugs, dist cap, rotor, and wires, repair bogie greasers (tire failure) 501.79 145628
08/08/13 AJM reconditioning and retinting all living area windows 1,000.00
09/15/13 AJM new house batteries – 2 6V golf cart batteries 200.00
12/292013 AJM installed surge tank for house water system 100.00
02/15/14 AJM installed new suburban 19K BTU furnace 500.00
03/15/14 AJM body work and paint – repair and paint SMC sides below waist to start 2,000.00

Installing a surge tank for house water system

Installing a surge tank for house water system

A long time ago (during the permanent bed conversion) I installed a Shurflo Whisper King water pump and have mostly been very happy with how quiet it is. The problem is that no matter how quiet it is, it is still audible when it runs. It makes us want to keep the water pump switch in the “off” position (very annoying) because it “burps” every 10 or 15 minutes. It doesn’t seem like much but some of us are sensitive to any noise when it is otherwise nice and quiet and it bothers us.

I figured it was happening because of a small leak in the built-in check valve in the pump. It turns out that a surge tank is listed as one of the solutions to this problem by Shurflo. They also recommend using a surge tank to prolong the life of the pump – so it doesn’t constantly start and stop. I found a nice sized (about 8.5″ diameter and about a foot long) at Home Depot’s web site (a Flotec FP 7105-8).

The photos below show a mock-up of how I planned to measure the pressure in the house water system (22 pounds with the Whisper King even though it claims 30 pounds in the documentation – I guess that could be because of a power issue, so I plan to check) and then to substitute the surge tank for the gauge. I held the tank in place against the back wall by adding a brace in front of it and connecting it to either side of the bed supports. The tank is held well out of the way of the rolling drawer that slides under there too – the horizontal line in the insulation  below the installed tank in the last photo is where the rolling drawer rests.

We plan to use the coach in the next month. I will report on if and how this helps solve our “noise problems.

Update 1/20/2014: We used the coach for a weekend trip – 3 nights – and the surge tank has fixed the problem of the water pump “burping”. We can now leave the water pump turned on when we are in the coach and there is no water pump noise except when the pump runs to refill the surge tank when we use more than around a gallon of water. When the pump runs it does so for about 30 seconds and then stops. Since it is a Whisper-King it is very quiet when it does run so, almost like home. Worth doing.

Re-skinning the bath and closet doors

Re-skinning the bath and closet doors

When I refurbished the interior living area in the summer of 2010 I did it in a hurry. The hurry was because of a self-imposed deadline for beginning a 7000+ mile trip to the East Coast and back again. Even though both doors had areas where the plastic laminate was not stuck to the aluminum frame I patched what I could with some new contact cement and skinned over the dark laminate with a real maple wood veneer also using contact cement. When we left on August 1st we headed east and everything looked great for quite a while but, once we hit the humidity of the East the wood veneer expanded and buckled. I have been trying to get around to it since returning from that trip. Now is the time.

The doors are made from an aluminum frame, skinned on either side with a Formica-type plastic laminate, and filled with a few blocks of particle board in strategic spots and expanded corrugated cardboard in the rest of the interior space. My plan was to remove either the veneer or the entire exterior of the doors depending on what worked. I had purchased enough new laminate (WilsonArt makes a natural maple plastic laminate that is a good match for real natural maple coated in polyurethane) to re-cover both doors so, when we returned from our last trip I removed the doors from the GMC and got started.

It turned out that the exterior laminate on both doors was loose enough to get off using a large paint scraper type of putty knife and a hammer (see the photo) with some gentle tapping. In one case the corrugated filler was completely loose and in the other it was stuck to the interior skin so I didn’t have to remove it. In that same case the interior skin was also loose enough to require re-gluing so I had to completely disassemble the door.

I cleaned the aluminum frame with a sander, added plywood pieces to the interior of the door where reinforcement was needed (towel racks on the bathroom door and a full length mirror in the closet) and reassembled everything using DAP non-flammable contact cement (I think it is better than the original one) everywhere. My only error was that when I reassembled the door that was completely disassembled I put it together with a slight twist to it. It still closes but that was not too bright.

Here are some photos that might be helpful: