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Returning from the GMCWS Rally at Temecula – better mileage?

Returning from the GMCWS Rally at Temecula – better mileage?

The coach ran so well with the new FiTech fuel injection system that we drove home without our normal overnight rest stop. Not that the trip is that bad normally, but with the constant stress of listening to the engine do its occasionally rough running – just short of fuel starvation – I hate driving all day. This time we drove the 9 hours with no trouble at all and I didn’t feel anywhere as tired as I normally do, even after a shortened day.

I measured the mileage for 1,062 “Barbie” miles (10% more than actual) and got 8.5 bmpg vs. my normal 7.0 or less. I will continue to monitor the mileage for a while to see if that holds true.

Other than how the coach ran I cannot think of anything else to report. The weather was very pleasant but not hot enough to tell if the “vapors” are really gone. Before our next trip I will be fixing the main waste tank valve and running a ground wire directly between the battery and the starter (a good suggestion from Ben Price at the rally).

Temecula, CA for the GMC Western States Spring 2016 Rally – Day 1

Temecula, CA for the GMC Western States Spring 2016 Rally – Day 1

Parked
We just finished the first day of our 59th trip in our “Barbie”-mobile and there have been several notable things happen already. Actually, it started on Friday morning when I started to get ready for our Sunday departure. We had dry camped for two nights at the Marana Bluegrass Festival and, since that was not a campground, the holding tank had not been emptied. Since I have a macerator pump I can empty the tank at my house using the sewer cleanout near the front door. I tried to use the pump and it did not work. It was frozen solid for some reason. I had to get it fixed so I ended up taking the coach back down to the storage lot, getting it up on ramps, and replacing the pump. Fortunately there is a great RV supply store in Tucson called Sandy’s West RV Center – they have everything, mostly in stock.

We left on time – 9:30 – but, just before leaving I tried connecting Carol’s computer to our inverter and it didn’t work. The inverter was putting out about 90-95 volts. It was the el cheapo from Harbor Freight and it had lasted more than 5 years. Well, we were planning on stopping in el Centro for the night and there was a Harbor Freight store there and, it was a 10-minute walk from the WalMart we decided to stay at – see the photo above.

The first day with the FiTech EFI went really well. It is having some issues with low speed response to the gas pedal – I checked with FiTech and it is learning. The guy suggested I try some “accelerator pump” settings but did not provide any hints for how to get started. I have asked for some samples and hints so we’ll see.

The biggest news was gas mileage. I have not been measuring mileage for the past couple of years because nothing ever changes it. The only modification I ever made that affected it was installing new mufflers. That probably increased my mileage by about 10% (measured over a 7,000-mile trip) – only because the old ones were bad and one was restricted. The point is, I know that I get about 7 MPG normally. When I stop for gas I stop based upon how many miles I have driven since filling the tank. I do not depend on the gas gauge, I put gas in about every 200-250 miles or less. When I start pumping I compute the approximate number of gallons I will need by dividing the number of miles by my average 7 MPG. It usually works and I’ll wait until it keeps happening before I get too excited but I could not get any more than 23 gallons into the tanks after I had gone 198 miles. That would be 8.6 MPG which would be amazing – I didn’t do it for the mileage, I did it for performance and reliability. Stay tuned.

FiTech Fuel Injection with Fuel Command Center Installation

FiTech Fuel Injection with Fuel Command Center Installation

This post is actually a compilation of some emails I wrote to a couple of other GMCers while the process was going on. Sometimes things are repeated but I did try to update a subject each time I mentioned [updates in brackets like these] it but it might still seem a little scattered. Sorry.

When we went to the GMCSJ rally at Tombstone we got the opportunity to talk to Jerry Work and see his FiTech EFI system. I took photos of his Fuel Command Center mounted on the passenger side of the radiator and then shot some photos of the throttle body with views of linkage and hoses. Those photos and one of the underside of my engine hatch are just below:

 

The following are separate sections, divided by day, that describe my progress.

I ordered my FiTech system soon after the Tombstone rally but the Fuel Command Center was backordered until March 15th. They did send it on that day.

On March 23rd I wrote the following:
I got the Fuel Command Center installed right where Jerry installed his. I used 1″ aluminum angle  to attach the FiTech-supplied brackets to the radiator housing instead of the white plastic panel in the photo of Jerry’s. But, installing the Command Center is as far as I got before I had to install 130 feet of baseboard in a rental house and the visiting grandkids arrived. The kids just left this morning. I have to finish the baseboards in the rest of the house – another 150 – 200 feet – this week while hosting Carol’s Mom’s 90th birthday party on Thursday. After those things are done I hope to install the EFI and then drive it to the Marana Bluegrass event on 4/8-4/10 [didn’t make that date]. If I don’t make that I will have to fit it in with my son’s visit a few days later. I definitely will have it in so we can drive to the GMCWS rally in Temecula.

The instructions look pretty easy except for drilling a hole in the exhaust pipe although Jerry said that was a piece of cake [it was. Just jacked up the right front side a couple of inches and removed the fender liner]. The instructions say that you cannot run the engine with the O2 sensor installed and no EFI working – it will damage the sensor. I confirmed that with the FiTech people. That means, if I want to be able to drive it, I have to be sure everything else is ready before cutting the hole or I will have to install a plug instead of the sensor if still using the carb.

On April 3rd I wrote:
I have the fuel “Command Center” installed and have the vent and fuel supply hoses installed on it and in place on top of the engine. I have run the wires from the six-wire harness to the places they go but they are not soldered in yet. I have run the display cable up under the dash but not in place – they supply a suction-cup stand to hold the display but I don’t know if the cable is long enough to use it. [I since moved the cable so it enters in the center of the dash and it is long enough for that].
I removed the carb and tried fitting the TBI onto the manifold but it turns out the general purpose throttle connection lever sticks down below the level of the manifold. Jerry Work said he cut it off but didn’t say how – my only option is a grinder. I sent a message to FiTech asking for advice if any. [Their advice was to use a spacer – I cut it with a grinder].
I also will be needing an adapter plate of some kind. They suggest a Summit Racing (SUM-G1420) which is only 1/8″ thick while Jerry Work used a 1/2″ thick adapter he bought at NAPA and then had to modify his hatch to accommodate it. I had hoped to get away with just the thick gasket I had under the carb but now I will be ordering the adapter after I verify that 1/8″ will work. [It turns out that I needed 3 adapters stacked with 8 gaskets – 2 from FiTech and 6 from Summit].
Some hardware for connecting the throttle and cruise control cables is also needed. Jerry got his at NAPA so Merle’s should have it too [They did not but I did find them on Amazon]. The numbers Jerry gave me for this are Manifold to throttle body adapter – NAPA 735-4930 [this adapter was too tall for my coach], Carb linkage bushing 1/2 to 1/4” – Mr. Gasket 6026 from NAPA, Carb linkage 1/4” stud kit (bolts through bushing on throttle body linkage to accept stock GMC throttle cable) – Holley 20-38 from NAPA. [I used the stud kit but it was too short to use both sides of the linkage bushing so I just used the back of it with the stud.]
I put the carb back on and now plan to get the TBI installed the week of the 11th so I can drive it a little before going to the GMCWS rally three weeks later. [Didn’t make that date either].

On April 13th I wrote:
I finally got back to working on the FiTech installation yesterday (Tuesday) and immediately found out that the FiTech guy who told me that I didn’t need an adapter plate was wrong – it was not even close. I started calling around and found one at Autozone but it was too thick – with gaskets it would be almost an inch thick. I called Don’s Hot Rod and they had one that was the same thickness. I had the NAPA number from Jerry Work for the one he bought so I called them and they said they could have it by 8:00am today so I said go.

When I picked it up I thought it looked a little thick but drove home anyway. I tried it on the coach – Jerry used it so it must work – but it ended up being about 3/4″ thick. It is actually closer to 3/4″ thick than it is to 1/2″. I put it back in the package and ordered 3 of the Summit Racing 1/8″ spacers that FiTech says work. My measurement of the space required for the butterflies on the TB is 3/8″ so three of them should work. I did think of making my own but, other than wood, I don’t know what material I could use. [It turns out that 3 of the Summit adapters was not quite enough but the addition of 4 extra gaskets that are included with the adapter plates and FiTech kit did the trick.]
I drilled a hole in my exhaust pipe for the O2 sensor yesterday and found that the clamps that came with the unit were way too big for my 2 1/2″ exhaust – they were too big for any normal exhaust pipe so I had to buy two more at Ace HW.
I have everything connected and even have the Fuel Command Center primed and ready. I even used my router to give the air cleaner another 1/2″ of space. As soon as I get the spacer thing fixed I will be able to start it up. My son is coming for a visit this weekend – arriving Friday – so I will not get to work on it again until Tuesday. Stay tuned.
On April 20th I wrote:
I ordered 3 of the Summit Racing adapter plates (SUM-G1420) that are 1/8″ thick each. I installed all three of them with one supplied gasket between each metal-to-metal joint and it was not quite enough so I added 4 extra gaskets (2 from adapter plates and two from FiTech) at the top and that did it. That did raise the air cleaner enough that I had to route out the forward portion of the engine hatch by 1/2″ deep and had to give it an extra inch forward. I bought 4 – 5/16-18 1 3/4″ bolts and torqued them to the 16 pounds specified.
On Saturday I installed the throttle body and connected all of the plugs and it started right up and ran nice and smooth. My son was visiting so I decided that was enough “fun” for the day and I shut if off. I locked up and turned the engine battery off and then thought about the installation instructions saying that constant battery power is required. That is so that the unit will have time to record its self-learning data. I turned it back on and went inside to look at the controller and, sure enough, it had been reset. I also noticed that the controller was on without the ignition key being on. I was informed by FiTech that this is normal and the alternative is to disconnect the controller connections (easy to do).
Besides starting the engine I was really anxious to see how the air cleaner and hatch cover fit. I immediately found that installing the fuel inlet at the rear left corner was a mistake – the air cleaner was hitting the inlet fitting. It turns out that the air cleaner has more room at the left front with the inlet pointing just aft of the alternator as usual and that fits fine. I left fixing the air cleaner for Tuesday when my son was leaving.
On Tuesday morning, after my son left, I finished making connections (the fuel vapor cannister hose is 1/4″ and the vacuum inlet is 3/8″) and moving the fuel inlet fitting. Now I installed the air cleaner – the FiTech unit requires a 5/16″ stud to hold the air cleaner and the top of my air cleaner had to be drilled out a little to allow it to fit. I just used a hex nut on the top, hand tightened. This is when I found out the the air cleaner is forward of the center of the recess in the hatch by about 1/2″. I had to enlarge that area and it now fits – I had to push down a little but I think that is due to the new weather stripping I installed at the same time. If necessary, I have a plan to add more space without a big lump in the middle of the floor. I hope I don’t have to use it.
Another problem I have identified is my fuel pump. I have only an electric pump installed just in front of the tank selector valve. A while ago, my mechanic noticed that the pump would not always turn on when the engine was started. I diagnosed it to be caused by the oil pressure switch which is there to shut the pump off if there is no oil pressure – i.e. the engine is not running. Gunning the engine a little just after starting was required. I noticed on the first start on Saturday that the electric pump was not running – the Command Center low pressure gauge was at zero. Given that the Command Center is holding somewhere between 1 and 2 quarts of fuel, a failed electric pump would take a while to notice. I bought a new switch and it seems to be working better.
I took it for a test drive today and I am impressed. When I first started driving there was a pretty familiar hesitation when going from no throttle to partial throttle but by the time I drove the two miles home via some stops and turns it was almost gone – self learning in action I assume. I then drove it to the NAPA store in Marana (to return the carburetor adaptor that Jerry Work used – too thick for my coach) and by the time I got back it was running great. Also, I will have to watch my speed on the highway because it wants to go faster than it used to – I love it. Now if my “vapors” problem is gone it will be worth the effort and money.
I had to buy 4 new bolts to bolt the TBI unit down to the manifold. I think they need to be 1 1/2″.

Bisbee for the weekend

Bisbee for the weekend
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This is the biggest change to the coach in quite a while. We have been using a single round table between us but the constant need to move the table when either one of us wanted to move around became a problem. The solution: make a table for each of us and add a little shelf to the storage cabinet for easily spilled items. The lamp and the cover (two holed panel) over the electrical connections complete that change. Like the lamp?

We had planned to make our first trip of this Winter to Prescott, AZ with the Saguaro Jetsetters but the weather forecast looked so bad we cancelled. Now that we were primed for spending some time in the coach – trying some new improvements to the living quarters – we decided on going to Bisbee, AZ instead. It is closer to home – only 2 hours vs. 5 hours – and the forecast was better – 15 to 20 degrees Fahrenheit warmer – so we decided to go there.

Bisbee is a very interesting town with lots of stuff to see. Here are some photos from this visit: 

The City of Rocks State Park – fun for kids of all ages

The City of Rocks State Park – fun for kids of all ages

The City of Rocks State Park is almost 30 miles Northwest of Deming, New Mexico and it is a pretty boring ride out there and back on the same road but it was worth it. That was the opinion of the kids – of all ages. Carol remembers her grandmother being there with the family when she was about 8 years old and there we were taking our grandkids there on Brooke’s 8th birthday. The park is really nice but most of the sites have no electricity. We were lucky enough to get two adjoining sites with electricity. It was fun for all of us.
From there we went home – with the rest of the family – completing our trip.

2015 Albuquerque International Balloon Fiesta

2015 Albuquerque International Balloon Fiesta

We got lucky and got some good weather for the balloon fiesta. We left the house at 5:15am and got to the first food vendor right at 6:00am. Cindy and Michelle’s house is just about 20 minutes away from the balloon field so we parked close and got right in. This is our second visit with them during the balloon fiesta. Our first visit was back in 2009 on our return from another GMCWS and GMCMI rally at Pueblo, CO. That year we had wind and it delayed the morning festivities and left lots of balloons out. This year we got very lucky. Here are our photos:

Santa Fe – crowded and not much fun

Santa Fe – crowded and not much fun

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This is “home” for a couple of days. A pretty rustic KOA Kampground just North of Santa Fe.


We have been here (Santa Fe) a few times before and each time we come we find it more crowded and less fun. The last visit was about 6 years ago so we figured some things had to change. The local tourist magazine said the new fun area was the Railyard area and we had not been there so that is where we started. All we wanted was a good cup coffee and some bakery food but we could not find that in the Railyard area. We got back in the car and took a drive around the old town area but it was jammed. The plaza, the heart of old town, was jammed – it did not make us want to park and walk around as we have done in the past.
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This is my driver. I drive the coach while she navigates. She drives the Tracker while I navigate. I am not as proficient with the tools though so it is not easy.


We headed back “home” around noon with the intention of heading back out in a couple of hours for a late lunch/early dinner. On our way back we passed two very crowded restaurants that were on the Old Las Vegas Highway where our KOA is. One closed at 2:00 so it was out but the other is open all day until 9:30 pm so that was our choice. Harry’s Roadhouse was crowded with locals and regulars. It has excellent service, a varied menu and good food. I had a small pizza and Carol had “an amazing smoked chicken quesadilla”. Highly recommended.

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The is the Santa Fe Railyard. It apparently was an actual railyard some years ago and while most of the tracks are gone, there are still passenger trains using these remaining ones.

Wind and fog – at least the coach ran good

Wind and fog – at least the coach ran good

We left Rapid City on Thursday morning with the objective of spending the night at North Sterling State Park in Colorado again. The park is 10 miles off of our planned route but it is quiet and we really liked it on the way north. The coach ran great all day and our only problem was the wind that was strong and gusting from our left all day. The good news is that the coach hardly minds the wind except for its effect on power and gas mileage.  We did make it to the park and spent the night snug as a bug despite the howling wind.

DSC02181On Friday morning we left for our next planned stop at Cheyenne Mountain State Park just south of Colorado Springs. Again this was our stop on the way to Rapid City and again we decided to spend two nights because it is so nice. Carol and Gordie joined us at the park again. The wind wasn’t as bad on Friday but the fog was terrible. It was dense fog the whole way – most of the drive was with about 1/4 mile visibility – pretty scary sometimes.

We spent the day Saturday resting and doing laundry. Carol did the laundry – the facilities are very nice – while I did a little maintenance. I fixed two rattling valances and cleaned the throttle and choke mechanisms on the carb – just a little spray can work. Also had a campfire with Carol and Gordie and their daughter-in-law and two really cute granddaughters. DSC02186

Sunday morning I discovered a tire was low on air – intermittent leaks? – and my Harbor Freight tire inflator quit while I was trying to fix it. I had to run down to O’Reilly and buy another one – this one is guaranteed for 3 years. The HF one was probably guaranteed for a month or so? The tire held up fine all day – I’ll check it again before we leave. Sunday night we are in Santa Fe but we don’t have cell reception. As strange as it sounds, all of the carriers except Verizon work here – Verizon cell phone don’t. Our internet connection through Verizon does work but it has the advantage of a roof-mounted cell antenna – I good idea from an old buddy named Dan Gregg.

Final day at the rally and some sightseeing

Final day at the rally and some sightseeing

DSC02175We got up and headed over to breakfast and hadn’t even finished it when I got a call from the machine shop that they had repaired my distributor. The name of the place is Johnson Machine and they are co-located with a NAPA auto parts store right around the corner from the fair grounds, so very handy. I got the distributor assembled and installed by 10:00 a.m. Makes me feel a lot better about driving again tomorrow. I bet I will be able to tell the difference.

After a long and boring club meeting and then a luncheon and raffle drawing – we didn’t win – we decided to take a ride to visit Deadwood, the location of Wild Bill Hickok’s murder, and Sturgis, the site of the annual motorcycle roundup (or something like that). It was a nice ride, we met a nice guy who owns a local deli – a friend of a friend. On our way back we passed right next to the Black Hills National Cemetery so we had to stop to pay our respects. When we got home we went out to dinner with Carol and Gordie at Murphy’s Pub and Grill – a very nice place with great food and excellent service. All four of us had fish and chips and it was delicious.

Rain, leaks, tech info, and general fun

Rain, leaks, tech info, and general fun
All dressed for Western Night at the rally

All dressed for Western Night at the rally

The weather went from too hot – even for South Dakota – to windy, rainy and foggy for two days. When I painted the coach I worked extra hard to find and fix all the leaky spots but I did miss a couple. Last year, after a little detective work I found and fixed the remaining leaks, but… Two more showed up just as we were preparing to leave on this trip. I didn’t see them leaking but the evidence was there with stuff that had been wet. One in the cockpit passenger side that doesn’t really hurt too much and another at the foot of the bed on Carol’s side. That one proved to be pretty bad and the corner of the bed was soaked the first rainy night. The next day we dried that out and did a small patch in a suspicious place and tightened the mounting bolts on the rear rooftop air conditioner. Meanwhile, when the rain resumed more detective work found the general area that was leaking and I managed to get it to drip into a container so we could stay dry. I think some dreaded silicone caulk will have to be applied to a couple more suspicious areas. Dreaded is because it is tough to get off and paint doesn’t stick to it.

One of our presenters was the builder of my distributor and I asked him about the pin that holds the mechanical advance weight and spring. As I think I said in a previous post, one of the pins came loose and the weight was not doing what it is supposed to. He suggested that the only way to fix the problem was to get someone to weld the pin in place. I disassembled the distributor again this morning and found the pin and the spring had both migrated to the bottom of the distributor and were stuck to the magnetic “pole piece” under the rotor – could have broken something in the wrong place. I took the piece and the pin to a local machine shop that is part of a NAPA store and they promised to weld it tomorrow morning. We’ll see.

All in all the rally has been fun. Lots of nice people and only a couple of bozo’s – don’t have any of those at GMCWS – and lots of GMC talk.